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펌프젯 추진기 날개 끝 누설 와류 감소를 위한 수치해석 연구NUMERICAL STUDY OF TIP LEAKAGE VORTEX REDUCTION FOR A PUMPJET PROPULSOR

Other Titles
NUMERICAL STUDY OF TIP LEAKAGE VORTEX REDUCTION FOR A PUMPJET PROPULSOR
Authors
김제인박일룡설한신정홍석
Issue Date
12월-2024
Publisher
한국전산유체공학회
Keywords
펌프젯 추진기; 프로펠러 단독성능; 전산유체역학; 날개 끝 누설 와류; 날개 끝 박리 와류; Pumpjet propulsor; Propeller open water performance; Computational fluid dynamic; Tip Leakage Vortex; TLV; Tip Separation Vortex; TSV
Citation
한국전산유체공학회지, v.29, no.4, pp 63 - 75
Pages
13
Journal Title
한국전산유체공학회지
Volume
29
Number
4
Start Page
63
End Page
75
URI
https://www.kriso.re.kr/sciwatch/handle/2021.sw.kriso/10566
ISSN
1598-6071
Abstract
This study presents the results of a numerical analysis using the Reynolds-Averaged Navier-Stokes (RANS) method to investigate the potential mitigation of tip leakage vortex (TLV) in the KRISO pumpjet propulsor through rotor tip shape modifications. Three alternative tip geometries were designed by extending the rotor tip toward either the pressure side, the suction side, or both. The present comparative analysis revealed that the pressure-side extension (PSE) tip achieved the most significant reduction in TLV compared to the original design. A detailed flow analysis in the gap indicated that the PSE tip effectively reduced both the pressure drop and velocity magnitude within the gap. However, the effect of the PSE tip on the overall efficiency of the pumpjet propulsor was found to be negligible.
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Jeong, Hongseok
지능형선박연구본부 (함정공학연구센터)
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